the timing was well out when I got the car, but I didn't spot it until after I lost pistons. I got a reasonable timing light to set the ignition timing to 15btdc, it then gave me a flat spot, but higher boost, so as a side thought I removed the hks actuator I had as it was sold to me as new but you never know type purchase, and put it back to stock with a view to installing the boost controller for the higher boost, even with the stock actuator I had more boost than I wanted, so I retarded the timing a little more and found the boost went up, I have now back to 15btdc and have a data log of the flat spot,
This is at 0.4bar boost with shell vpower.
rpm and ign timing are on the right scale, the timing is pulled from 4000rpm, and the VTC is turned off at 5700rpm according to the log file
This is a slow rolling start as shes auto