Just an update it was the filter on the catch can stopping up. Ran the hoses back to the intake like stock setup was and everything is doing fine. Ive put almost 4k miles on it since and not losing any oil or coolant. I have since installed a nistune board and new coil packs. I also found out that the acc, o2 and vct were not getting a 12v power. Last owner pulled the fuse for it and i also found he broke a bolt that held the acc valve on the intake. Had to pull the intake off to fix that. It was a lot easier to pull off that it was to get on. It also has a new starter from a 65 datsun 411. Getting ready to buy new injectors, dump pipe, down pipe, maf, bov, and turbo. Still trying to decide what turbo to go with so the dump pipe is on a waiting list till i decide what turbo.