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joshuaho96
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Everything posted by joshuaho96
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R33 RB20E not revving
joshuaho96 replied to liam.fredricsen's topic in R Series (R30, R31, R32, R33, R34)
Blocking the return line you probably broke the fuel pump or something similar. Dead heading a pump requires very careful pump control to regulate the pressure. -
That really sucks. I was a little unsure about the tool set but checking the actual tool listed in the manual it’s the same general idea: I suspect the valve springs are part of the problem but it seems kind of shocking that you could so easily mar the bucket with the pliers like that and also damage the edge. It’s not like dealer techs are particularly careful either.
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Start by searching for a boost leak/vacuum leak. That is the first port of call if your idle is weird.
- 14 replies
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- boost leak
- splutter
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It's not that hard. Many parts are sold direct through Nissan USA dealers now, just look up the part numbers through the parts catalog. The 260RS is entirely R33 GTR as far as drivetrain goes.
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It's probably fine to set a conservative rev limit like 4000 RPM. On the street you really don't need more revs/power than that. That way if the sensor is broken and reporting a false 0 pressure signal you can still drive the car, but on track if it is accurate you're forced to calm down and investigate the issue instead of just hoping for the best and possibly spitting conrod bits all over the track.
- 212 replies
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- migrate-from-302-euro-discussion
- bmw
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Freshly Rebuilt rb25det no compression!!
joshuaho96 replied to Driftieboy's topic in R Series (R30, R31, R32, R33, R34)
It is possible to refurbish the cooler, in the US at least we have some oil cooler service companies that are mostly specialized in aviation and are FAA certified. Those oil coolers are usually huge, huge money because everything in aviation is. They flush the cooler under pressure and high temperature + ultrasonic it until they verify that the cooler no longer sheds debris. -
SR20DET - TURBO (GBC22-350, GT2560R OR GT2871R)
joshuaho96 replied to timmy94's topic in General Automotive Discussion
Like I said earlier, it's smaller than stock. You can just look at the numbers and compressor map to know this. Technically the turbine will flow more due to higher trim but the compressor flows less air at the same pressure ratios. -
SR20DET - TURBO (GBC22-350, GT2560R OR GT2871R)
joshuaho96 replied to timmy94's topic in General Automotive Discussion
The GT2560R is quite literally the factory 91F00 S15 turbo. So size appropriately from there. -
He already asked this question earlier on a Facebook group, I have the same turbos and in 4th gear it should be at 10 psi around 3200 RPM. Uneven compression across the the cylinders is not a good sign, especially by that much. I would also question the cam timing, it's possible the cam centerlines were not cut correctly or some other issue with the aftermarket cams, supposedly Brian Crower has QC/QA issues.
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Isn't the RB25 NEO a shim over bucket engine? In every shim over bucket engine I've seen you use a special service tool to depress the outer rim of the bucket and then use a magnet and a thin plastic spudger or something similar to pull the shims without undoing the cams precariously like you did. When I check the R34 service manual that's also what it depicts:
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Yeah, it's very contextual. If you have to add a bunch of plumbing and general annoyance to "do it right" then I also wouldn't bother. On the RB26 venting directly to atmosphere means capping another port on that combo vaccum/coolant pipe under the plenum and figuring out how to keep track of a random hose/hose clamp 5+ years into the future. I have a mystery "firewall harness bolt" sitting in an organizer and it's taking up a non-trivial amount of my mental headspace trying to work out which of the five or so cars it could possibly have come from.
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Turbo pressure line is the green line from the plenum. Almost all diagrams online just vent to atmosphere which is why you're confused. This is fine on speed density systems but it will cause an unmetered air leak on MAF-based systems. Even if it's nominally ok you really don't want to make a habit of it because it just makes it harder to diagnose what's wrong in the future.
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Factory solenoid is 2 ports only as others have said. To make a two port solenoid work you must tie the wastegate line to the plenum (boost source). That way when the solenoid isn't working the engine just makes wastegate boost. Then when the solenoid activates it vents to atmosphere (blue line). When you vent to atmosphere the problem with a 2 port solenoid is two-fold. First, it's a boost leak which is annoying. Second, you really want the pressure experienced by the wastegate to be as low as possible. With a 2 port solenoid the wastegate line will always see a pressure higher than atmospheric because the turbo's boost is bleeding both to atmosphere and into the wastegate line. The 3 port splits the two states. Either you are sending boost pressure to the wastegate line (solenoid is off) or you are venting the wastegate line to atmosphere (solenoid is on).
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I'm a big fan of more advanced modeling so it's easier to constrain the problem and there's less opportunity to shoot yourself in the foot. As OP mentioned you know when you're really screwing something up when working with a VE model if the numbers don't make any sense. 100% VE at idle for example. X-Tau constrains the problem of transient throttle such that you're only picking a wall-wetting constant and time constant and everything else just flows out from there. If your wall wetting constant or time constant is some ridiculous value you know you're doing it wrong.
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I'd have to look at the series 2 in specific but when I worked with the EMS-4 in AEMTuner it did not work in speed density. Yes it uses manifold pressure as a load signal and there is an IAT/CLT sensor that is used to adjust fueling but all the tables ultimately operate in raw injector pulse width, it has no conception of volumetric efficiency.