yeah I really dont think trp was responsible for the bodgy work on the head conversion,i.e the roughly tapped head stud threads,the buggerd up tensioner relocation,
the thread tape and sealant used to try and hide the oil leaking from said tensioner...the block/bottom end was certainly new,
but as said before was damaged beyond useable and likewise the crank,by whoever put the 26 head on and fitted the clutch..no way a shop like TRP would do the long list of rough as gut crap we found in this motor..