After some last minute, late night shenanigans my car finally got back on the road (after 6 months sitting in the backyard). What should have been a quick tune turned into a 6 hour adventure, with the std GTR injectors maxing out, then a hidden CAS ground wire becoming unearthed and not being discovered for 90mins (we thought the CAS died, and were awaiting a replacement to be delivered).
There was no EBC fitted as I wanted it to be wastegate only, but there seems to be some funky problem with the wastegate holding boost - even wound in fully to 1.2 bar.
Car's mods:
Custom spaghetti low mount turbo manifold
HKS 3040 .73 A/R
Trust type R wastegate
Greddy plenum
Aftermarket metal head gasket (unknown thickness)
Q45 t body + AFM
Trust 115mm intercooler
Sard 700cc injectors
HKS 256 + 264 reground copies (have a master now, can do these at will)
Full 3 inch Nismo exhaust, no center muffler
Will be setting up an SBC ID 3 tonight for another late night marathon, the car was detuned from this run to cope with additional boost, and more low rpm boost as well.