I've had my car (1998 R34 GT-T + Power FC + 3.5" Exhaust turbo back + GTR intercooler + K&N Pod Filter + Walbro Fuel Pump) for 18months now and have had an insignificant surging problem at idle ever since I purchased the car. (Read on - gets worse)
(Background info - The timing belt was claimed to be changed by the previous owner at 44,000km, which was 30,000km ago)
I finally decided get rid of the bleed value it came with (eekk!!!) and have recently installed a Apexi AVC-R boost controller to properly maintain the 14psi at full boost (stock turbo). I also have had a trusted turbocharging specialist (popular on supra forums) dynotune my Power FC hand controller as I had altered the timing map myself over the last 18months to completely eliminate pinging that was occuring on boost due to a terrible tune it had when i purchased it.
THE ISSUE IS
On the dyno an issue arose by where the power fc or prehaps a sensor will lean out the timing map by where the air/fuel ratio of 12.7 will intermittently increase to as high as 19 all on its own and then return back to normal. (very similar periodic behavior to the "insignificant surging problem" I was having pre-tune, however now that the car's tune is pushing the limits of its performance the "insignificant problem" is now very significant in the sense that I would usually need to switch off the car or give it WOT to correct the problem of the leaning out (It feels like a dog to drive when its in that state)
The timing belt was not an issue as we adjusted the timing belt adjustment bolt on the dyno yet it still did the intermittent leaning out problem.
Because it comes and goes randomly I am having major issues diagnosing it.
What are your thoughts?
Could a faulty sensor be responsible for its periodic leaning out behavour? Power FC at fault? Please Help!!
DYNO RESULTS (for your interest)
The dyno results (done at NT Performance (Footscray, VIC)) are attached (before and after)
You'll notice the blue line has two dips in it.
One very noticable at the 115km/h mark and one at the peak power of 235rwkw due to a slippery clutch which only started happening on the dyno due to the freak power the engine was able to produce thanks to NT Performance.