Well after some Friday arvo beers I managed to Gee the boss up pretty hard, basically I stressed that there was no point in us going out to get kicked off for a mid 10, let's try to run a 9....
So, I came back around 30 seconds later with a 6262SP in hand and it didn't take much convincing. Friday was a party here at Powertune, music cranking, cashews, chips, and within a very short time the turbo was on and the Red Dragon was getting reversed onto the rollers.
Had a solid 5 passes on the dyno, but we knew the 6262 needed a bit more boost to get it in the zone, though 45psi didn't agree with something in the engine! It filled number 2 and 3 with water so we're thinking it's either lifted the head again or cracked the block around a water jacket.
Anyway, I've rocked up here this morning and the engine is out, and 2.2L stroker in ready to go, in fact they're finish up the install of the built engine now with the 6262SP on. Get ready for round 2