Jump to content
SAU Community

Recommended Posts

Hey guys,

I just had an 80,000km service done on the line, as well as having the exhaust manifold gasket done and the car feels like its lost a lot of power, throughout the whole rev range..

I have it running on 0.80 Bar (i think thats what the AVCR measures in), however it simply will not push over 0.61 since the service.

The car is also extremely quiet, exhaust note wise - however i put that down to me being used to the mild exhaust leak, although it might be quieter than when i bought it.

Service guide followed was the 80,000km one listed in the Gen Maintenance forum

Iridium plugs -> NGK Platinum

Castrol Edge oil still.

Turbo Gasket, Exhaust Manifold gasket + 3 studs.

I have a PFC, which i put the hand controller in tomorrow, what things should i be looking for (besides knock).

Would the 80k service include removing any advance (forgive me if this is electronic, i'm used to old holdens) that may have been set by guys who originally tuned it (ice down in melbourne)?

The workshop did a great job, but they don't specialise skylines so i'm trying to give them a heads up if anything thats a quick fix, or risky.

Cheers,

Link to comment
https://www.sau.com.au/forums/topic/151063-post-service-loss-of-power/
Share on other sites

check the timing. Perhaps ask them if they adjusted anything at including the timing.

There is a remote possibillity that an exhaust gasket (any of the ones put in) was out of alignment when bolted down, the factory ports aren't well matched for a start. Do some looking about 'after' checking the obvious timing and plug gaps.

Irridiums are a waste of money by the way. Go the copper plugs. NGK 6BCPR6ES etc..

Check that the vacuum lines are hooked up correctly.

Is this in regards to the Boost Controller?

I have an Apexi AVCR. Now its maxing at about 0.6 kg/cm2 which i think roughly works out at 7psi (or stock), the AVCR is still reading what the boost is (i assume), is it possible that its not doing its thing with the wastegate (forgive me, i'm not sure exactly how it works).

what would i look for to see that this isn't the problem?

I've chatted with Marc this morning, but unfortunately didn't grab my PFC Hand Controller (~5 hours sleep last night, late shifts) to check anything there - But the guys who worked on it, mentioned that Vacuum Hoses hooked back up and that the Gaskets fit very flush (both Marc and the mechanic were surprised about this).

I reiterate that the car isn't misfiring, and in general power delivery is smooth, just not anywhere near as oomphy as it was.

Thanks for the help so far,

Edited by nsanity
Is this in regards to the Boost Controller?

Nope, all of them. You will have the signal for the boost controller, the hoses between the solenoid and the actuator, the hoses to the bov, the hoses to the charcoal canister. There are lots of them.

Some one who is not familiar with what goes where may get something backwards accidentally.

It's just a thought. Timing may have something to do with it aswell as has been mentioned.

Is it surging in the higher rev range( 5000-7000rpm)?

Timing can be an issue.

Raz

forgive me, explain surging?

The car simply Plataeu's in performance (it has a very stockish feel to it - not that i ever drove one, to break traction off the line, you have to dump it at 4-5k, rather than simply just plant your foot in first) at around 3-4000rpm.

doesn't feel like its being starved (i've driven cars where the fuel pump isn't up to the job, doesn't feel anything like that) - Boost hits 5 on the Dash (0.6 on the AVCR) and simply just hard lines there.

If i can have stuff to take to them on wednesday when i settle the account, hopefully its just something quick.

I thought timing would be all electronic? i didn't give them the PFC hand controller, nor do they have the equipment otherwise.

almost sounds like an exhaust restriction.

when you say it plateaus does it go hard up untill a certain point then taper off or is it flat all the way through the rev range?

before i found out some prick at an exhaust shop had welded a bit of box section steel (bout and 1" square) in the tail pipe of the rx7 the car would pull really hard till about 5-5500rpm then would die in the ass. once i had it removed the car would rev to 9000 easily.

im using this as an example by the way not as a plug for rotaries :happy:

almost sounds like an exhaust restriction.

when you say it plateaus does it go hard up untill a certain point then taper off or is it flat all the way through the rev range?

before i found out some prick at an exhaust shop had welded a bit of box section steel (bout and 1" square) in the tail pipe of the rx7 the car would pull really hard till about 5-5500rpm then would die in the ass. once i had it removed the car would rev to 9000 easily.

im using this as an example by the way not as a plug for rotaries :happy:

Think of it as if all of a sudden you couldn't get the throttle more than half-open. I still get to 7k rpm (i change between 6.7-6.9 when driving hard), but the feeling just isn't there.

Thats the feeling of loss.

sidenote - why the f**k would someone weld shit in your exhaust? noise?

Thanks for all the replies, i'll get them to check the vacuum hoses, and the timing on Wednesday.

Edited by nsanity

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • Middle seat good for a slab of beer or Esky for a road trip. 2x kids, means 1x free seat lol.
    • So we have most the interior back in, and for the first time with one OEM speaker hooked up. The 31 is running, driving and now tunes!!! Hahaha yet another step for the sub that sat 10m under for two weeks!!! unbelievable really 👌 lots of love work and not giving up on her. Seen so many youngsters part way less, and in way better condition. I’m stubborn, thinking another problem is just a hurdle to overcome, One at a time. IMG_9277.mov
    • That is correct. I'm using a modified ABS ring and a ZF speed sensor on my rear diff for speed input. I'm running a Haltech ecu. 
    • Been busy with the newborn. We originally thought we were going to go for a third, but we're good with two lol. He's starting to actually sleep now so I've had some energy to work on the car. It's been parked away in the garage since late November due to winter.  I went ahead and redid all my head oil drains. I originally had my front and rear head drain going into the same pipe but have since split them up. I also added an Ethanol content sensor to get ready to run E85 this summer. Tossed it on my return line. Sensor sits nicely under my intake manifold.    I also have a lot of parts that came in for my rear end. I'll be swapping over to a 3.3 final drive and doing the GK teck anti squat mod. While the rear subframe is off, I'll also change every bushing. We're planning on buying another house soon with the condition that I get at a minimum a 2 door garage, so I'll wait to have more room for this. Now onto the strange things that recently happened... After changing the lower rad hose (It had been sitting in my cabinet for well over a year and was the last hose I had to replace), I let the car idle in the garage to bleed my coolant. After running for a few minutes, it started missing. Got much worst within a minute or two and then stalled and would not restart. My crank sensor decided to crap itself. No damage, no explanation, just died. I went ahead and replaced it with another ZF sensor but the heavier duty stainless model with a shield. Tossed that in and started right up. Has anyone else seen this? I hate when things fail without cause. Luckily this was a blessing in disguise... This lead me to recheck my timing. It seems I may have had a beer or two the last time I had set my TDC angle as I was off exactly 5 degrees... I miscounted a line haha. I was running 5 degrees less then commanded. It's a little embarrassing but helps explain why my dyno operator seemed to think I should be making more then 478rwkws.        
    • Sharing results from recent Liberty Walk R35 GTR, since they are still considered as somesort of a V36 Skyline. We do them turbos too. This are high flowed SS-1 models with ball bearing conversion done.  Car have managed to pull 485awkws @ 20Psi so far pushing limitations of factory built engine. The build list for R35 GTR enthusiasts as follow : HyperGear high flowed stock turbos in SS1 (G25-660 specs) Custom titanium intake pipes. Vspec performance titanium front pipes. Vspec performance 4" titanium exhaust. Upgrade fuel pumps. 1200cc injectors. Ignition coilpacks Hks intake plenum. Hks intercooler piping. Greddy intercooler. Greddy bovs. Top-secret coolant reservoir. Emtron ecu. Straight E85. Built gear box.  
×
×
  • Create New...