Jump to content
SAU Community

Recommended Posts

Hey all just popping in real quickly again to ask the opinions of the forum. Car is a 95 gts-t with fmic, pod with cai, 3.5" turbo back exhaust split dump, running 12 psi with an ebc, always run 100 ron fuel, plugs gapped at .6 or .7, stock everything else and afc neo. Now I was watching my afr's the other day at full throttle and without a tune on stock ecu the reading I got was never below 11 is that common for a skyline with these few mods? Now I'm thinking the readings are definately off cause while at idle I never get anything below 16 just want to confirm that the wideband is stuffed, when at full throttle I never get anything below 11 and I had the wideband exposed to exhaust fumes and heat for like a week before I got power to it. All help is appreciated and welcomed. Thanks again in advance. Also a friend of mine has a ca18 that he wanted to get 300 - 350 rear wheel hp out of and I was wondering if you guys could help out or point in the right direction car is virtually stock and its an automatic.

Link to comment
https://www.sau.com.au/forums/topic/192302-is-this-heard-of/
Share on other sites

it cant hurt to get your readings checked against a calibrated 5 gas analyser.

Also those WB02 sensors are very sensitive to exhaust leaks.

Unless your exhaust sytem is 100% sealed then your readings are worthless

I think all skylines with stock ecu's do it once you add boost, thats why so many people get s-afc's to get that extra power, mine runs down to 10.5ish on full throttle!! although I haven't run it again after putting in a new 02 sensor. but I wouldn't stress about it mate >_<

Silly question here.. is the AFC actually tuned?

A tune of the AFC would resolve this... being thats what they are used for

Nismoid thats why I am asking the question, not silly at all ,I'm thinking its a bit high for an untuned skyline on stock ecu.With the mods I listed thats a whole lot more breathing room for the engine so I was expecting 10's at least, another mod I forgot to mention is a bosch 040 fuel pump recently installed like 3 months back, also fpr with gauge and stock pressure reads 44 psi at idle without vacuum. At idle also the widebands reads and shows nothing less than 16 and goes all the way to lean as the car warms and in closed loop mode still nothing less than 16 just was wondering if this is common or can I say the wideband is stuffed come on you don't find this a bit strange. Now i can't say my exhaust is perfect but there are no leaks I can visible hear or see.

I think a few people have missed the point. The 02 sensor should be keeping the AFR at ~14.7 in closed loop as Fat is saying. Usually it would be a bit richer at full throttle also.

Most likely either:

1. Stuffed measurement device (AFRs its reading are wrong)

2. Stuffed fuel pump

3. Stuffed Fuel pressure regulator (check fuel pressure at rail at idle)

4. Stuffed O2 sensor (Doesn't explain only 11:1 AFR at full throttle - usually would be richer)

4. Stuffed AFM (less likely)

Edited by benl1981

if you want good ratios, you need a tune.

02 sensor has little to do with it most of the time. thats why some people run it without that feedback. also the ratios depicted may be inacurate depending on where the wideband is installed in the exhaust and the piping size. any leaks (which many cars have) makes it even more "guessy"

11s is not that rich anyway

That's what he's saying - he expected it to be running richer than that. Mine was in the 9-10s when I upped the boost which is usually how they go.

O2 sensor is what sets the AFRs at light load and idle. In fact I can drive around town in closed loop most of the time if I baby it round. The tune has to be close to the mark first but then the 02 sensor will bring it back to 14.7 AFR by playing with the injector duty cycle.

Take it to a dyno and pay $50 to get it checked there both on idle and full throttle, then if its the measurement device you havent wasted your time trying to fix a problem that isnt there.

Edited by benl1981
I think a few people have missed the point. The 02 sensor should be keeping the AFR at ~14.7 in closed loop as Fat is saying. Usually it would be a bit richer at full throttle also.

Most likely either:

1. Stuffed measurement device (AFRs its reading are wrong): Really think so either the wideband O2 is stuffed or there is a leak in the exhaust cause I did all the test on the device to troubleshoot it and everything was spot on

2. Stuffed fuel pump: Brand new bosch 040

3. Stuffed Fuel pressure regulator (check fuel pressure at rail at idle):44psi

4. Stuffed O2 sensor (Doesn't explain only 11:1 AFR at full throttle - usually would be richer): Maybe read that if you have them connected without power to it might stuff it up and i did for like a week thats the wideband tho have a narrowband on the way that I will install ths week

4. Stuffed AFM (less likely): Could be but doubt it

That's what he's saying - he expected it to be running richer than that. Mine was in the 9-10s when I upped the boost which is usually how they go.

O2 sensor is what sets the AFRs at light load and idle. In fact I can drive around town in closed loop most of the time if I baby it round. The tune has to be close to the mark first but then the 02 sensor will bring it back to 14.7 AFR by playing with the injector duty cycle.

Take it to a dyno and pay $50 to get it checked there both on idle and full throttle, then if its the measurement device you havent wasted your time trying to fix a problem that isnt there.

:Wish I could but dynos are rare over here would fix a whole lot of shit but have to wait a month before they bring the dyno back!!! :rolleyes: You all know how it is once you get someting you want it perfect right away just don't have the tools man so I gatta eliminate stuff on my own really think its a leak tho with the seal around the gaskets of the decat pipe might be my mind but think I can hear a little air escaping will get that siliconed also the dump pipe area and move the wideband O2 sensor to just before the deact pipe tis weekend and see if that fixes it.
it cant hurt to get your readings checked against a calibrated 5 gas analyser.

Also those WB02 sensors are very sensitive to exhaust leaks.

Unless your exhaust sytem is 100% sealed then your readings are worthless

Hey Thanks all found the prob as you stated they are very sensitive to exhaust leaks. There is a hole the size of my finger right above the wideband O2 sensor bung half assed welder didn't weld it properly. Gonna get it welded shut on the weekend hopefully this person does a better job and I can finally tune the car properly.

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Latest Posts

    • Initially I thought having a pair of Recaro seats would be a big bonus, it turns out these do get a little uncomfortable on long journeys (my fault, not the seat). I had a look through the GSM Performance website at reclining seats and booked an appointment to visit their show room. I got the Recaro Sportster CS for the R34 from here, was very happy with the service received so of course a re-visit was in order. Unfortunately the two Corbeau seats I had chosen aren't on display but they had 4 other options available. Two seats dug into my back, one dug into my legs and the other was perfect. I also found out that Recaro seats use a larger bolt pattern so some adaption was required. Luckily GSM offer some universal adaptors that should solve this problem. I searched the interwebs for price comparisons and Corbeau themselves were the cheapest at £300 cheaper (for the pair). I asked GSM if they could price match, unfortunately they couldn't. I later received an email saying Corbeau would honour them the same discount, but the purchase was already made. I did however order the brackets from GSM, both arrived on the same day. I started with the passenger side seat, knowing this was going to be a little trial and error. There are 3 mounting holes at the front and 2 at the rear on these JURAN Racing seat rails.  With the adaptor brackets mounted, the allen cap bolts started to push into the seat, NOT GOOD!  The rear mounting holes lined up but there were issues at the front. The holes were 1/2 hole out, so the brackets got a tickle with the drill to modify the holes. The supplied bolts weren't going to be long enough and a spacer was needed to stop the adaptor bars from bending. A local fasteners company supplied be with some nylon spacers and longer bolts (M8x30, although these will be replaced with 35mm long shortly) A before and after I pre-drilled the front bracket before making a start on the driver's seat to save some time. And in no time at all that was in the car too. The all black seats have transformed the interior and these are MUCH more comfortable. The only downside with the new Corbeau seats is I sit a little higher, but I'll happily accept that over discomfort. The Youtube video can be found here: https://www.youtube.com/watch?v=wPyttKPktXA
    • All 3 I guess. The car came with the JASI Aero 4 door Type R Full Kit unpainted so this was one thing at the top of my list to complete then I noticed there were body panels parts for this kit so i picked them up along with some black mesh to fill in the front bumper and front side air vents. car is at a paint and body shop atm completing this work. Next I will be addressing the internal bells and whistles, great summer project I can do with the kids.  full interior removal - ,boys car sound deadening - pads and spray ,boys stereo, sound, lighting - Big 3, GTT or bigger alternator ,kids head lining - dye black add star lighting mod ,daughter. That's it for the next 5-6 months. I have some motor maintenance  work i have to plan out. oil filter relocation, gaskets, mounts. beyond that, mind is starting to turn over if i can use a DET intake plenum, block off turbo ports & pipe in a air intake.      
    • roller coaster of a ride. Alarm system was removed & main harness was repaired where possible. still no fix just random successful starts. moved on to the replacing the ignition switch and relay. well all this troubleshooting & repair has been going on, the car is at a paint and body shop being pushed around. Ive been going down there on odd days after work to get it sorted.     
    • 5th November if you want to come out for a spin wakfield
    • PROBLEM WAS BROKEN COOLANT SENSOR!!! Replaced with a new one and its running mint.
×
×
  • Create New...