Jump to content
SAU Community

Recommended Posts

Fuuuuuck, cars on the trailer ready to go. Had some 'issues' with fitting the R33 GT-R wheels on the front as they just knicked the strut *ffs*

Anyone coming out to Mallala tomorrow that could bring out a pair of bolt on spacers I could maybe borrow for the day?

I possiably have a mate that is going home to try n swap his bolt ons with a slip on to make sure all clearances but just covering all bases!

Love you all - hahaha

Thats why i run 27mm bolt ons on the front of the ceffy. Rubs on the strut like a bitch.

  • Replies 14.2k
  • Created
  • Last Reply

Top Posters In This Topic

Heyas

Well a few of u guys know that I've been having "issues" with my gtr for the last year or so

figured out it was due to incorrectly set factory TDC value on the cams, which had been hacked in the ecu to get it to run right (thanks Century20...asshats)

heres a rundown of the last few months

Firstly, Car had std everything, was pulling 210kw at 14psi when i bought it, which was normal. after a couple of years the stock injectors started to leak, and that forced me to buy new ones, so I figured a cheap upgrade would be worthwhile - 575cc upgrade was cheaper than 444cc, however this necessitated a retune and for a retune to be possible, a nistune daughterboard was required.

Before I had the nistune, my mechanic reduced the fuel rail pressure to lean out the flow so it wasnt running so rich which was great. I got some economy but it was still running too rich to get decent power... this did 180kw but it was running stupendously rich - this is the tune I went away to loxton on, dion and krishy can attest that i was blowing tonnes of soot out the rear end

Then I got the nistune daughterboard installed and took the car to boostworx for a tune, shaun's standard gtr image was loaded and adjusted for the bigger injectors and the nismo afm's id installed the day before. he said that he felt the cam timing was out, perhaps by a tooth... best he could manage was 130kw

took the car to road & track, they took off the head and discovered that the TDC marking on the cams were between 3 and 5' out and that the previous ECU tune (before nistune) was set to compensate for this - so the current tune isnt quite right - the timing shaun had to adjust to fix the prior poor cam timing needs to get retuned to stock, and im fitting N1's within the next fortnight, so that would also require a remap - in short won't be getting a retune at boostworx till everythings mechanically sorted however I'm back to similar power levels as before and the response is shithouse, loads of flat spots in the power curve - in spite of that, i can hear the turbos spooling up MUCH quicker than before which is always a good sign - in either case, the adjustments to the cam setup at road and track got me back to 180kw while running rich - we're going to fit the n1's and see how the fuel map scales from 0-20 psi as opposed to 0-14psi

to break it down

2007 - bought gtr, 14psi = 210kw

2009 - dynoed after injector replacement, 180kw (put down to rich mix)

2010 - after nistune, 130kw put down to totally munted timing and enrichment map

- cam timing reverted mechanically, 180kw at 10psi with same tune as above

- estimated 210/220kw on stock turbos at 13/14psi (wont bother with this)

- estimated 300kw on N1 turbos at 20psi with correct ignition timing and correct fuel map

more info to come as i mod the bugger

-D

LOL Weez.....you're gonna give yourself a coronary (not a canary) before you get out there................breath in, breath out :)

I just about did last night haha :P

Day went well and car didn't miss a beat all day long!

Guest
This topic is now closed to further replies.



  • Similar Content

  • Latest Posts

    • Latest round of updates on the car. I purchased and installed a SWS clutch slipper to help with 60ft times and got some second-hand good condition 275/40R17 Hoosier DR2 radials. Test and tune in November showed the tyres were an upgrade over my over 15 year old mickey Thompson's and I got a 1.8 second 60ft and pb et of 11.71 but even then, that run wasn't great due to rain and driver error (the event got called off 10 minutes later fast forward to the weekend just gone 25th of Jan and there was finally a break in the weather to let racing happen. The first run the track was slippery and only managed a 12.1@129 Second run the track was better and got a new pb et and mph: 11.54@131   Lith and I then worked out that I installed the previously mentioned clutch slipper incorrectly and its never been working, and I had just been dumping the clutch the entire time, we also noticed it was on street boost and not race boost. So I lined up for a third run with the car turned up in the first two gears, but the passengers side axle objected to clutch dumps and left the chat which stopped my weekend.   so there will be another attempt in the future once I replace the tyres as they rubbed and are stuffed now. but a low 11 should be on the cards.
    • Ceramic coating and heat shielding, you mean?
    • Turbos don't require pulling the motor apart so that's "easier". I would recommend the Nismo R3 turbos instead if you want to do stock twin turbo. It doesn't make as much power as the 2530s but it's only like ~50 whp off the mark and should have better response (ball bearing CHRA, slightly smaller turbo). A local that went with a Garrett G30 and 6boost manifold recently nearly burned his car to the ground after the hood insulator started melting and and burning so if you go single turbo I recommend doing a lot of research and validation work to make sure you don't do the same.
    • New rear lights, filler panel sprayed, cleaned and back together    before, during, after shots 😍
    • 100% is gyprock, I agree. Slip of the keyboard. Haha! I left my indicator bulbs out to save a bit of weight.
×
×
  • Create New...