Jump to content
SAU Community

Recommended Posts

Car in question is a R33 GTS-T only mods are a front mount, CAI and a larger exhaust from the cat back (so I dont think it would really affect the back pressure)

So my car has been boosting to around 12psi no matter what setting I put the boost controller on... I removed the apexi boost controller and put a new hose with new hose clamps straight from the wastegate actuator to the intake piping. Car should be running 7 or 8 psi now like stock.

Anyways it still overboosts, I can hit 12psi in any gear if I plant it, im sure it would go more but the car starts to miss or backfire and starts acting all jerky.

Does anyone else have any ideas of anything else to check before I replace the wastegate solenoid?

Link to comment
https://www.sau.com.au/forums/topic/311283-wastegate-actuator-problems/
Share on other sites

Its an L shape. Comes off the side of the wastegate heading to the side of the car then it bends heading towards the front.

kind of looks like this one http://www.nissanparts.cc/catalog/nissan/R...SM%20NPLOGO.jpg

Edited by ascenion24

I cant for the life of me find a replacement actuator, all the generic ones have a straight pushrod and it wont clear the turbo outlet...

anyone got ideas?

Does the standard actuator pull apart so I can replace just the spring or do I have to replace the whole assembly?

Edited by ascenion24

I cant for the life of me find a replacement actuator, all the generic ones have a straight pushrod and it wont clear the turbo intake...

anyone got ideas?

Does the standard actuator pull apart so I can replace just the spring or do I have to replace the whole assembly?

Edited by ascenion24

Has always done this since Ive had the car, which has been only a couple of weeks. I thought it was the boost controller not working properly so I removed the boost controller and it still over boosts.

I can move the actuator rod with a pair of pliers, But I dont know the limits of how much it should be able to move, it could be getting jammed and I dont even know.

Actually Ill move it by hand and measure the throw, then ill put compressed air to it and measure the throw. If the throw is less with the air then the actuator is stuffed. If the throw is the same then something is stopping the wastegate from opening completely and will probably need turbo out to inspect.

Am I on the right track here?

hmmm... just ran a test.

Hooked the air comp up to the wastegate and the rod moved the same amount that I can move it by hand. (If I grab the rod with pliers I cant move it I have to grab the connection at the turbo and twist, should it be easier to move?)

So it seems as if the swing valve is getting stuck, but its a stock system so I cant see anything being in the way.

I'm not sure what to do here, the test wasn't exactly scientific so not sure if I can rely on it.

What should I do?

Edited by ascenion24

Personally I'd try taking the c-clip off the actuator arm at the end where it kind of bolts onto the gate, then see if you can turn the little flap easily enough by hand, it should just be loose as anything.

Just to rule anything out at that spot.

Will give it a try tonight, how much should the wastegate move from closed position?

I drew a quick diagram to help explain, the diagram shows the lever in the closed position, should it be able to rotate only 45 to the vertical? or upto 90 degrees? etc...

Thanks.

post-25219-1268266164_thumb.jpg

Hey mate, going from memory I think it's more like this, but I could be wrong..... I didn't take much notice last time I had it off

Whether it's 90* or 135* I'm not sure, but it's definately in that area

post-58284-1268281091_thumb.jpg

Edited by mosquitocoils

Sounds silly but have you checked to see if the Restrictor is still in this pipe????

restrictorhere.jpg

If not get the tappered end of a bic biro and stick it in there that should stop it over boosting

Edited by jjskyline79

Restrictor what?

I've replaced the pipe with a new piece of fuel pipe to make sure there were no leaks.

So without the restrictor it would overboost?

Ill check the old pipe.

Also do you need the restrictor when using an aftermarket boost controller? When I had the apexi hooked up it was still over boosting.

Edited by ascenion24

If you want to run the higher boost, try gapping your plugs closer together. The standard coils can't deliver enough spark when there is higher boost so blows out the spark. If you reduce it to 8 mill gap if i remember correctly this should give you enough to run the higher boost.

Not the problem but hey :cool:

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • Jdm DC2R is also nice for a FF car compared to the regular hatches of the time.
    • Now that the break-in period for both clutch and transmission is nearly over I'd like to give some tips before I forget about everything that happened, also for anyone searching up how to do this job in the future: You will need at least 6 ton jack stands at full extension. I would go as far as to say maybe consider 12 ton jack stands because the height of the transmission + the Harbor Freight hydraulic platform-style transmission jack was enough that it was an absolute PITA getting the transmission out from under the car and back in. The top edge of the bellhousing wants to contact the subframe and oil pan and if you're doing this on the floor forget about trying to lift this transmission off the ground and onto a transmission jack from under the car. Also do not try to use a scissor jack transmission lift. You have to rotate the damn thing in-place on the transmission jack which is hard enough with an adjustable platform and a transmission cradle that will mostly keep the transmission from rolling off the jack but on a scissor lift with a tiny non-adjustable platform? Forget it. Use penetrating oil on the driveshaft bolts. I highly recommend getting a thin 6 point combination (box end + open end) wrench for both the rear driveshaft and front driveshaft and a wrench extension. These bolts are on tight with very little space to work with and those two things together made a massive difference. Even a high torque impact wrench is just the wrong tool for the job here and didn't do what I needed it to do. If your starter bolts aren't seized in place for whatever reason you can in fact snake in a 3/8 inch ratchet + 6 point standard chrome socket up in there and "just" remove the bolts for the starter. Or at least I could. It is entirely by feel, you can barely fit it in, you can barely turn the stupid ratchet, but it is possible. Pull the front pipe/downpipe before you attempt to remove the transmission. In theory you don't have to, in practice just do it.  When pulling the transmission on the way out you don't have to undo all the bolts holding the rear driveshaft to the chassis like the center support bearing and the rear tunnel reinforcement bar but putting the transmission back in I highly recommend doing this because it will let you raise the transmission without constantly dealing with the driveshaft interfering in one way or another. I undid the bottom of the engine mount but I honestly don't know that it helped anything. If you do this make sure you put a towel on the back of the valve cover to keep the engine from smashing all the pipes on the firewall. Once the transmission has been pulled back far enough to clear the dowels you need to twist it in place clockwise if you're sitting behind the transmission. This will rotate the starter down towards the ground. The starter bump seems like it might clear if you twist the transmission the other way but it definitely won't. I have scraped the shit out of my transmission tunnel trying so learn from my mistake. You will need a center punch and an appropriate size drill bit and screw to pull the rear main seal. Then use vice grips and preferably a slide hammer attachment for those vice grips to yank the seal out. Do not let the drill or screw contact any part of the crank and clean the engine carefully after removing the seal to avoid getting metal fragments into the engine. I used a Slide Hammer and Bearing Puller Set, 5 Piece from Harbor Freight to pull the old pilot bearing. The "wet paper towel" trick sucked and just got dirty clutch water everywhere. Buy the tool or borrow it from a friend and save yourself the pain. It comes right out. Mine was very worn compared to the new one and it was starting to show cracks. Soak it in engine oil for a day in case yours has lost all of the oil to the plastic bag it comes in. You may be tempted to get the Nismo aftermarket pilot bearing but local mechanics have told me that they fail prematurely and if they do fail they do far more damage than a failed OEM pilot bushing. I mentioned this before but the Super Coppermix Twin clutch friction disks are in fact directional. The subtle coning of the fingers in both cases should be facing towards the center of the hub. So the coning on the rearmost disk closest to the pressure plate should go towards the engine, and the one closest to the flywheel should be flipped the other way. Otherwise when you torque down the pressure plate it will be warped and if you attempt to drive it like this it will make a very nasty grinding noise. Also, there is in fact an orientation to the washers for the pressure plate if you don't want to damage the anodizing. Rounded side of the washer faces the pressure plate. The flat side faces the bolt head. Pulling the transmission from the transfer case you need to be extremely careful with the shift cover plate. This part is discontinued. Try your best to avoid damaging the mating surfaces or breaking the pry points. I used a dead blow rubber hammer after removing the bolts to smack it sideways to slide it off the RTV the previous mechanic applied. I recommend using gasket dressing on the OEM paper gasket to try and keep the ATF from leaking out of that surface which seems to be a perpetual problem. Undoing the shifter rod end is an absolute PITA. Get a set of roll pin punches. Those are mandatory for this. Also I strongly, strongly recommend getting a palm nailer that will fit your roll pin punch. Also, put a clean (emphasis on clean) towel wrapped around the back end of the roll pin to keep it from shooting into the transfer case so you can spend a good hour or two with a magnet on a stick getting it out. Do not damage the shifter rod end either because those are discontinued as well. Do not use aftermarket flywheel bolts. Or if you do, make sure they are exactly the same dimensions as OEM before you go to install them. I have seen people mention that they got the wrong bolts and it meant having to do the job again. High torque impact wrench makes removal easy. I used some combination of a pry bar and flathead screwdriver to keep the flywheel from turning but consider just buying a proper flywheel lock instead. Just buy the OS Giken clutch alignment tool from RHDJapan. I hated the plastic alignment tool and you will never be confident this thing will work as intended. Don't forget to install the Nismo provided clutch fork boot. Otherwise it will make unearthly noises when you press the clutch pedal as it says on the little installation sheet in Japanese. Also, on both initial disassembly and assembly you must follow torque sequence for the pressure plate bolts. For some reason the Nismo directions tell you to put in the smaller 3 bolts last. I would not do this. Fully insert and thread those bolts to the end first, then tighten the other larger pressure plate bolts according to torque sequence. Then at the end you can also torque these 3 smaller bolts. Doing it the other way can cause these bolts to bind and the whole thing won't fit as it should. Hope this helps someone out there.
    • Every one has seemed to of have missed . . . . . . . The Mazda Cosmo . . . . . . what a MACHINE ! !
×
×
  • Create New...