Jump to content
SAU Community

Recommended Posts

Nope, but they are multiple speed. I've noticed mine kick in at a couple of different speeds.

Those of us with programable ecus also have the ability to maintain a chosen temprature as well. Mine is set to come in at 93 degrees. You'll know vq25dets run considerably hotter.

When the car is moving at speed it is largely irrelevant IMO. But your clutch fan probably heat soaks your intake some more :P

One thng I noticed is that with a big rad, there is loads more airflow through the engine bay at speed, and it washes the hot out too.

But your clutch fan probably heat soaks your intake some more :P

Really....not while the car is running.

P.S. You might find that the big frying pan on top of the VQ35GLASS heat soaks a lot more......even with NA power!

  • 2 years later...
  • 1 year later...
On 11/11/2012 at 5:20 PM, bigkevracer said:

In the US, a popular mod on VQ35 powered cars has been the coolant bypass kit. Originally used on the VQ40 powered Nissan Pathfinders as part of their towing pack, the kit removes a blanking plate in the middle of the valley of the V6, allowing coolant to flow easier, and more coolant to pass through the radiator. This in turn lowers water temps.

Scotty nm35 developed a VQ25DET specific version of this bypass mod, to account for the turbo piping on the DET engine. At the same time he ditched the standard air bleed valve, a plastic pile of rubbish, and replaced it with a metal version with a tap for easy filling and bleeding of the cooling system.

So it was off to the super secret Pure Motorsport workshop for the install...

2012-11-10%2013.45.26_0.jpg

By day, a busy heavy vehicle and diesel repair business owned by my parents. Much like a good mullet, the front is for business:

640-2012-11-10-10.05.04.jpg

But the back is for party. This is where I usually work on the car, lucky to have access to a hoist and tools. Sadly my usual spot was currently occupied by my little sister's Audi 80, which was having it's soon-to-blow engine replaced.

640-2012-11-10-13.42.23.jpg

So a makeshift service location was setup behind the Safari-spec Jackaroo.

large_2012-11-10%2013.43.19.jpg

Looking down at the motor, the first step if you have to is to remove the cover of the engine, so you're left looking down at the plenum chamber:

2012-11-10%2008.19.03_0.jpg

First up, remove the hoses connected to the plenum and the four bolts and two nuts which hold the plenum down.

2012-11-10%2008.31.56_0.jpg

Next up, we'll need to remove everything fastened to the plenum. Start by removing the holts on the blow off valve return pipe, attached to the plenum:

2012-11-10%2008.36.33_0.jpg

Undo the bolt fastening what appears to be the bracket for the transmission dip stick.

2012-11-10%2008.38.28_0.jpg

Remove the three plugs to the right of the plenum chamber, and the two bolts which fasten it to the side of the plenum.

2012-11-10%2008.44.07_0.jpg

Undo the nut on the standard boost controller.

2012-11-10%2008.45.50_0.jpg

Undo the hose clamp on the throttle body, and unclip the wiring plug from the throttle body.

2012-11-10%2008.47.38_0.jpg

Remove the hose on the back of the plenum chamber.

2012-11-10%2008.47.57_0.jpg

Then simply lift the plenum straight up and off the studs. You'll be left with something like this:

2012-11-10%2008.57.57_0.jpg

It's a good idea to cover up the centre bores - you don't want to drop anything down into the engine.

Next up, we'll need to remove the fuel rail. There are two bolts on each side of the rail:

2012-11-10%2008.58.09_0.jpg

Once you've removed the four bolts, remove the plugs on the right hand side (air intake side) injectors. You'll then need to carefully lift the rail straight up to remove the injectors from the block. When you lift the rail, be very careful not to loose the o-rings and plastic retaining rings around the tips of the injectors.

Lift the fuel rail up and carefully pull it back onto the left hand side. I was able to hold mine in place by placing the blow off valve on top of it:

2012-11-10%2009.03.18_0.jpg

Remove the four plastic spacer rings that sat underneath the fuel rail mounting points and set them aside. Then you can undo the six bolts that hold that piece (injector manifold?) in place which will give you access to the valley:

2012-11-10%2009.12.30_0.jpg

Great success!

Now you can see the blanking plate we want to replace with the cooling mod, at the back of the block in the valley. Simply remove the four bolts fastening it down:

2012-11-10%2009.15.33_0.jpg

Then place silicone on the bottom of the new plate. The clear silicone can eat away at aluminium, so we used grey silicone. You can bolt the new plate straight down to the block.

2012-11-10%2009.29.16_0.jpg

You'll then need to put together the return hose. Insert the Proflow fittings into one end of the hose (you may have to heat up the hose), then fasten the supplied hose clamp onto the fitting.

Now this is where I made a mistake, and here's tip 1:

Tip 1: Don't trust Scotty's measuring.

Scotty was a bit too generous for his own good and supplied a bit of extra hose. All good, but it'll save a lot of headaches later if you take this opportunity to measure the hose from the block to where the tap will be (you will see the stock plastic bleed point in the heater hose behind the stock fuel pressure regulator). Trim the hose and drop the hose clamp over the hose, then insert the Proflow fitting (again, heat the hose) and tighten the clamp.

Connect the Proflow fitting to the plate on the block, and tighten it down. Make sure it's tight so you don't have to do the job twice!

2012-11-10%2009.55.22_0.jpg

I took this opportunity to give the injector manifold a clean in the kero bath, which isn't necessary to do:

2012-11-10%2010.04.20_0.jpg

You can then place the injector manifold back onto the block, and fasten it down. Dad caught me doing this and overtightening the bolts, which leads me to tip 2:

Tip 2: Don't over tension the bolts. Use a tension wrench to tension to 34NM.

I was quickly handed a tension wrench set to 34NM:

2012-11-10%2010.15.57_0.jpg

You can then insert the injector rail back into the manifold, and start tightening it down. That's when this happened:

2012-11-10%2010.37.28_0.jpg

Shit.

It looks like the bolt had cross threaded or binded and it just sheared.

A quick phone call to Andrew at AM Performance, and he told me he was at work, and able to have a look at it for me. I jumped into dad's parts hack and drove over there straight away.

2012-11-10%2011.22.58_0.jpg

Andrew set to work welding up the manifold and getting it ready to go. He was really happy to drop everything and help me out.

2012-11-10%2011.23.29_0.jpg

He was in the middle of helping a customer with a 4 door R32 replace the motor with a freshened up RB20.

2012-11-10%2011.23.39_0.jpg

Andrew was able to weld the manifold back together and get me back on track.

2012-11-10%2012.13.04_0.jpg 2012-11-10%2012.13.06_0.jpg

Andrew tells me that this is a common problem with Nissans, and gave me Tip #3:

Tip 3: When reassembling the engine, use high temperature thread lubricant.

I used a copper based Loctite product that dad keeps in the workshop.

I rushed back to the workshop and set to work putting the car back together.

After bolting the intake manifold down and tensioning to 34NM, I reinstalled the fuel rail and carefully torqued down the bolts to 34NM, or in the case of the repaired thread close to 34NM.

2012-11-10%2013.01.16_0.jpg

We then set about removing the hose clamps on the heater hose around the stock plastic bleed valve. The constant tension hose clamps were in the wrong location to be easily removed, and the stock plastic tap broke in the process. We also replaced the constant tension hose clamps with worm drive clamps just to make it easier to remove in the future. We fitted the tap between the heater hose and attached the Proflow fitting from the block to the bottom.

2012-11-10%2013.01.27_0.jpg

Thanks to the size of the new tap, we noticed the heater hose rubbing on the body and decided to cable tie it out of the way just in case.

2012-11-10%2013.01.07_0.jpg

You can then reinstall the plenum, working in reverse to the above removal steps.

Finally, bleed the cooling system. I chose to start the car, and carefully open the tap. There was a rush of never ending bubbles. I close the tap and waited until the thermostat opened, and reopened the tap, running it until the bubbles stopped. It only took a matter of seconds.

So I guess the next question is: Does it work?

I've seen two key benefits to this mod, which are exactly as suggested by Scotty:

  • Bleeding the cooling system is now rediculously easy. Run the tap until no more bubbles. Doesn't get easier than that. I suspect this mod will really come into its own when you need to perform top ups of the cooling system, which I'll find out for myself in a couple of weeks when I replace the radiator and hoses.
  • Coolant temps have dropped significantly. I noticed a 5 degree drop in coolant temps before and after. This may not seem like much, but ambiant temperature rose 10-15 degrees between before and after. I expect in like for like conditions you'd be about 15 degrees better off.

 

So remember the three tips so you don't bugger up the install as I did:

  • Don't trust Scotty's measuring.
  • Don't over tension the bolts. Use a tension wrench to tension to 34NM.
  • When reassembling the engine, use high temperature thread lubricant.

 

http://performancewa...ass-mod-install

Any way to restore the pics in this Ryan ?

No i bought mine from aleks when he stripped his car but yes its scottys cooling mod.

All up took me close to 5 hours as i installed the radiator and thermostat as well and bled it like 4 times.

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



×
×
  • Create New...