Jump to content
SAU Community

Recommended Posts

Car is down over 20kw since the last time it was on this very same dyno. I have replaced a blown head gasket in recent times. Not using coolant, no head gasket symptoms since fixing it.

Same boost, same AFRs, CA18, T28BB.

I have changed the intake cam though, to a CA18DET exhaust cam, I have just gone over the timing again and counted the cogs between the marks, all is spot on as per the FSM, base timing is 10 degree.

It makes more power and more torque than it did previously up until about 4000rpm when it just falls over.

Before it made 180rwkw, now it's struggling to make 160.

I've got acompression tester coming to check and I've just had an idea that maybe the butterflies aren't working, would it make that much difference?

At the moment both cams are set to zero as I hae adjustable gears, don't wanna change them just yet.

Ideas?

Comp test first you have changed a fair bit of things that could be causing it so logic says you did something wrong, I had a issue on my audi and couldn't find it so re did everything I touched and it was all good , my bet is something to do with cam timing but I don't really know those engines but on rb26 a restrictive cat will cost 20 kw easy .

Scott

Is the cam swap a proven drop in upgrade or are you somewhat of a guinea pig working on fair assumptions?


Coz if the later I would assume the physical cam timing needs to be redialed...

Did you use stock gasket or bigger (1.2-1.6mm)

If you used bigger gasket you have lower compression so will need bit more boost to make up for the lost compression!!

Sorry guys, SAU wasn't giving me updates.

I was working on this issue here if you want the full rundown.

http://www.nissansilvia.com/forums/index.php?showtopic=532583&st=0

Comp test was fine. Turns out I had the butterfly actuator connected backwards. I'm fixing that then will see how it runs.

I quadruple checked the cam timing again and it looks fine, the advance one tooth trick is for people who don't have gears but that's where the bulk of the power comes from so I have adjustables.

This is a tried and tested path.

Cheers for the responses.

Edited by ActionDan

In a CA the exhaust cam is 248 duration and 8.3mm lift and it's a direct fit on the intake side as well, which is only 240/7.8.

On It's own, not a huge upgrade, but coupled with adjustable gears it's worth up to 15rwkw mid range and top end.

Especially helpful if you have a larger turbo like I do.

I've just finished putting it all back together. Will post pic tomorrow.

I'm fairly confident it's right because it only fits on that side resting on the pin with the shaft in one position.

With the shaft in any other position other than fully CCW the lever won't attach and be resting on the pin comfortably.

I got under the car with it running and the actuator stayed put, I couldn't spin it up and be under it though but I think it's right now.

Those cam gears look spot on to me too.

I'll test drive it when it's not raining.

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • I can see between the water jacket and cyl 3 there wasn't a hard line of combustion gas. It certainly appears that the issue is coming from there. Yes, checked the tension. All at 100ft lbs where I set them 5 years ago. These blocks can crack but generally when they have been over bored. Mine is only 0.5mm oversize at 89.5mm. They break between cylinders around the 91mm mark. No sign of that with mine. My gut feeling is the head gasket lifted a while back when the studs stretched and i bandaided it by retorquing the studs. It's finally let go.
    • My Nismo 1.5 churps a bit on reverse turns when cold, but besides that feels like a stock diff.
    • Yes, but, I paid cash and I'm pretty sure the receipt was in the bin 10 minutes after I got home Note to self, keep all receipts
    • Bunnings would have just handed you your money back on that one!
    • So, version 4 intake is on its way I was looking at these a while ago but at around $200 or more it was a little pricey for something that might not work, but, I had it in my watch list, but, I got a message saying it was on special, and I had a code thingie to use, it eventually came in at $120 delivered, so BAM, BUY NOW.....LOL I'll need to have a look when it arrives but I feel it will "look" better than what I currently have, as it comes with a PCV fitting, so I will be able to get rid of the alloy pipe that goes to the throttle body with the PCV fitting  Well, that's what the voices in my head are telling me  Oh, and this happened today Yeap, it was a Trojan, and it was cheap, so I headed back to the hardware store and actually spent a little bit more on a heavy duty,  one that was actually recommended by a plumber mate, a Cyclone one with a fibreglass handle that is actually rated for clay The broken shovel will eventually be "modified" into a short handle shovel
×
×
  • Create New...